The Big White Bus Will Not Start (Post #625) September 25, 2023

spark plugs

In this post I am sort of after the fact prepping the motor for it’s first start in several years (at least 3 years). I was given some advise that I should lubricate the cylinders prior to starting for the first time. The reason is obvious. The cylinders are dry.

I’ve already tried to crank the engine. That was evident in the last video. So perhaps doing this NOW is a bit superfluous. Meaning I’ve probably already damaged something. But maybe not, I’ll know when I get the engine started.

I’ve pulled plugs and I’ve squirted some WD-40 inside each cylinder. How much you say? That’s a great question. I was told at least a couple of seconds of spray. The WD-40 fluid is going to adhere to the cylinder walls and if the rings were stuck, would have acted on them hopefully freeing them. They make a special “foggy spray” for this application but I was told just to use WD-40. I highly recommend you do your own research on this. I’m damaging my own stuff. I don’t want you to damage your stuff if I’m wrong.

The fuel pump is on the way and might arrive today 9/25. That would make it 8 days since I ordered it. They don’t work on Saturday or Sunday so Monday was the first time they started to “fullfill” the order. I am also in the farthest away region from their shipping hub. So a minimum of 5 days of transit. Looking at their location, I could have driven up there, picked up the part in person, and arrived back at base camp before the shipped part arrived.

Next step is to get a fuel pump installed and the Big White Bus started. Drive it to the top of the driveway. Hose off the parts so I can coat them with rust conversion paint. I will then turn her around and have the starboard side on the same side of the shoppe as the welder. I have some rust under the starboard rear wheel well the might need some patching. I also have the repairs to the existing rust spots identified in other videos. B pillar, D pillar.

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Thanks for reading and Happy Rovering.

The Big White Bus Will Not Start (Post #624) September 18, 2023

Fuel pump

Well, awesome. The Big White Bus won’t start.

I have fired it up once since I parked it in my newly constructed shoppe 5 years ago. I guess I should have expected there would be “issues”. But I wasn’t expecting the issue to be this one.

Mr. Fisher came over and we diagnosed the issue. We started with checking the power at the pump. As you may be aware, when you turn the key over it powers the pump briefly. So if you just “turn on the key” and go back there to check the voltage you won’t find any. That’s why it takes either some seriously creative use of a volt meter or you get one of the bestest friends to come over and turn the key for you. We had voltage all the way through the wiring harness.

We then confirmed we have spark from the ignition system. I pulled the number 1 plug and with a screwdriver I grounded it and watched for spark. You can buy a fancy spark tester, matter of fact I think I own one. I have no idea where it is though. Spark confirmed.

So we have two of the three things (Meatloaf would say that “ain’t bad”) to make the vehicle run. Air and Spark. Now why aren’t we getting fuel.

I pulled the gas line off at the regulator on the back side top of the engine and had Mr. Fisher crank the ignition. We should have had gas squirting out if it worked. It did not. This fit with me NOT hearing the pump run when the ignition was turned over.

The only thing left was to pull the fuel pump and do a visual inspection. What I found was not expected. I said, “Wow.” a lot in the video. There were several parts that were obviously degrading due to being submerged in petrol for so long. There was visible rust on the steel parts as well. Generally the pump was in a terrible state. I was not aware that petrol would do that to those parts. The only gas I ever put in my Classic is 100% real gas, unless I am in Texas where they only sell ethanol (at least the last time I was buying gas there). You would expect ethanol to eventually separate and turn to water. You can read all about that on the Road Guardians website.

I will be replacing the fuel pump and have ordered the part from Atlantic British. I found some that were cheaper on Amazon. But my skepticism and need to have it delivered before next October weighed heavily on my decision where to purchase. The pictures all looked like the pumps were manufactured in the same place. Same white plastic. Same blue plugs.

Fuel pump
PRC9409K

If you look on Amazon you’ll see the pumps look like the same ones. If I had unlimited funds or sponsorship, I’d buy one from everyone and do a side-by-side comparison.

All this “BUY IT NEW” has me thinking about what this would cost if we just fixed the pump. All you need to do is replace the pump in the collector can (that bottom part). I’ll do a post about that in the coming weeks.

So…do I drain the tank too? If the gasoline HAS turned to varnish I should probably put some treatment in there. I’m thinking I’m gonna add a silly amount of STP Fuel Injector cleaner in that tank. I can say, WHEN I get it running It will run for quite a while before I shut her down. I want to give the truck plenty of time to dislodge any crap in the fuel lines. I’m also guessing I’ll need to swap the fuel filter too.

If its not one thing, its another. It really, never ends.

Mr. Fisher also brought over his Viair Compressor. We spent some time looking at it and checking out all its features.

Thanks for reading and Happy Rovering.

Fender Repair Part 5, MORE Crappy Welding of the Large Fender Patch (Post #622) September 2-3, 2023

Super happy

In this installment I finish the left rear fender panel. And by finish I mean I had to completed replace the outer fender I had previously welded up. I added a strap to attach the inner fender to the outer fender.

The outer fender’s welds were compromised because I ran out of shielding gas halfway through. The panel was 16 gauge and I swapped it with an 18 gauge. The right thing to do was replace it and “do it right”.

Now, I’m no body man and right to me is probably not right to someone who actually knows what they are doing. As I mentioned in the video I need another 10 or 20 years of welding experience to be “competent”. Over all I’m a lot happier with this replaced panel. The 16 gauge panel would not have worked. It would not have been watertight no matter what I did.

I covered everything with yet another coating of primer. I also put seam sealer in the appropriate places. This only seemed prudent as I am almost certain this will rust again. My hope is it will take at least 20 years to rust out.

I thought some of the welding went a lot better than the previous attempts. I want to say, “I’m getting better.” but I’m pretty sure I’m fooling myself. Most people could probably weld if shown how and a little practice. Welding WELL however is really hard.

So add to the fact I’m saying welding is hard…and welding UPSIDE DOWN is another level. We did not go over this scenario in my class. I’m half tempted to take the class again and do the entire class upside down. I finally figured out the I could weld sideways that worked pretty good. Even with my new sideways technique it didn’t stop me from getting some new holes in my PPE and my skin from hot slag dripping down. My grandson Grady was horrified by the scab in the crook of my elbow. The chunk that got me on the chest made a similar hole there.

I also did quite a bit of cutting and the sparks flying back on me warmed me up a bit. Thankfully my Round House Overalls1 deflected the sparks and only “warmed” my family package. If you remember this post from December 2010, “The one where I catch myself on fire in the furtherance of Land Rovering” [Okierover] I caught myself on fire cutting the passenger side floor panel. What I learned from that was:

  • Blue jeans are not safety gear and are a sad substitute for PPE.
  • Longjohns [IBC] (aka long handles [Collins], thermal underwear, etc…) will keep the flame off you for a brief time.
  • Your best friends don’t want you harmed, but also want to take videos of you when you are on fire so they can tease you later.

Thanks for reading and Happy Rovering

1This is my unsponsored review of Round House Brown Duck Overalls. It is a solid 10 out of 10. They are made in Shawnee Oklahoma (Home of Brad Pitt) and at $60.00 a pair (on sale at the time of this posting) a real bargain. 

Fender Repair Part 4, Fixing My Crappy Welding of the Large Fender Patch (Post #621) August 27, 2023

The weather cooperated, but my back didn’t so much. The temperature was mostly pleasant compared to the scorchers we’ve had lately. My back however was not very cooperative. I’m pretty sore after just a few hours of work.

The work on the fender from the last post was, pretty terrible. I had trouble shaping the 16 gauge steel. The patch after shaping was also the wrong size. Couple that with running out of shielding gas and my welds being pretty terrible, I needed to start over. Without shielding gas protection you have a brittle weak welds. Not to mention holes in your weld called porosity.

I cut the patch out with a cutting wheel. Some of the welds were actually pretty good, so I must have run out part way through the welding. I made a patch with a piece of paper and cut out a new patch out of 20 gauge steel. When I was getting the shielding gas at Chickasha Industrial I noticed they had a lot of steel in the shop area. Turns out they sell steel. So I picked up a few “cutoff” pieces for a good price.

The new patch with some help from a ingenious use of a 2×4 and a bottle jack fit nicely. I welded it in and it worked out pretty well. I struggled with one spot when the welding blew through a thin patch of original fender. With some creative welding I got the holes patched.

I still have to weld up the underside. Welding upside down is difficult. I’m going to have to figure out how to do that. Maybe watch some Youtube videos or something.

I will use the 16 gauge steel to reinforce the 20 gauge and weld in the seat belt mount. I don’t plan on having seat belts in the rear again but if I did, I’d need a place to mount them.

Thanks for reading and Happy Rovering.

http://Patreon.com/Okierover

Shoppe Clean-Up and Mower Repair (Post #617) July 31, 2023

Broken Mower Part

No Land Rover content this week. I started the weekend trying to get the chores done first. Mowing the grass which grows at a ridiculous rate due the the wet July we’ve had. I’m cutting grass every week now.

I got on the mower and got my book on tape going [Extreme Measures by Vince Flynn the eleventh book in the series]. I kept hearing some odd noises, vibrating parts, and the engine was running like crap. Just last week I was evaluating how many more summers I might get from this mower while I was patching the holes in the tires with plugs.

I have been impressed at how trouble free this mower (Husqvarna 1842) had been with this being the sixth summer. I’ve only had one other serious repair. It was also a mandrel. I have also replaced one battery and before the summer is up, I really should replace all the tires.

After an inspection I saw the shaft on the mandrel wiggling like crazy. The upper bearing failed on the mandrel. So it wasn’t going to be grass cutting for the weekend, it would be mower repair. I looked the part up and found it had a John Deere part cross referenced. I went down to P&K Tractor on Highway 9. The parts guy was SUPER helpful. He looked up the part on several sites and found a part number at O’Reilly’s. Turns out in his words this was the most common bearing in the world. I was surprised how many different parts numbers were associated with it. I ran down to O’Reilly’s grabbed two.

The bolts (steel) were really stuck in the mandrel housing (cast aluminum). You don’t have to be a chemist to know this is a recipe for disaster. And that’s exactly what happened.

I wound up having to attempt to drill and easy-out what was left of the bolts. Broke two drill bits and eventually the mandrel. Four hours lost. I’ve ordered a replacement, it comes in this week. So I spent the rest of the day cleaning and organizing the shoppe.

I’m going to visit an old Marine friend of mine this week. Jeff was one of my closest friends in the Marine Corps. We went to boot camp together and artillery school. I haven’t seen or heard from him since perhaps 1988. Gonna be great catching up. RovErica’s kids are coming to stay with us this week too. With all this happening I don’t think there will be any video next week. But we’ll see.

Jeff and Bear
Heavy sigh.

Thanks for reading and Happy Rovering.

Fender Repair Part 1, Welding Patches (Post #616) July 25, 2023

Welding a patch for the body mount

I finally broke down and welded something on my Range Rover. While I will admit freely, I am NOT a welder, but I did enjoy getting the patches welded on. I took a few hours the day before this video was shot to “practice” welding with some scraps I had cut off the Big White Bus.

One of the difficulties is the metal on the Range Rover and the metal I am patching with are different thicknesses. I believe the OEM body panels are 18 gauge whereas my patching material is 16 gauge. I watched a YouTube video where a young man from Weld.com showed how he setup his welder to weld different thicknesses. It’s pretty good stuff and I recommend it if you are still wondering how to setup your welder and what settings you might want to start with. His settings for 18 and 16 weren’t different so I just need to find the same settings he suggested and convert those values to the letter equivalent on my Lincoln MIG Pro 180.

I also watched a fellow from Make It Kustom that has some great tips on welding and patch making. Good stuff there too. This guy is obviously an artist and I imagine has, “done this a time or two.”

In my video there is a lot of grinding and sparks flying and hopefully some good tips to help you weld your patches on your Range Rover Classic. I sped a lot of it up so I’m not consuming a lot of your life watching my low grade videos.

The camera overheated at the end for the second time that day. The temp inside the shoppe was above 110°F (which is 43.3°C for you metric system types). Yeah that’s pretty hot for this old man. I’m seriously going to investigate getting an exhaust fan installed to pull the hot air out.

Overall I’m pretty excited that I can weld stuff. I did fix a yard swing that one of our trees landed on and crushed. I’m looking forward to finishing the welding on the rust and turn my attention to making stuff like a 270 degree awning, a rear bumper, and lots of other stuff.

Thanks for reading and Happy Rovering