Fender Repair Part 4, Fixing My Crappy Welding of the Large Fender Patch (Post #621) August 27, 2023

The weather cooperated, but my back didn’t so much. The temperature was mostly pleasant compared to the scorchers we’ve had lately. My back however was not very cooperative. I’m pretty sore after just a few hours of work.

The work on the fender from the last post was, pretty terrible. I had trouble shaping the 16 gauge steel. The patch after shaping was also the wrong size. Couple that with running out of shielding gas and my welds being pretty terrible, I needed to start over. Without shielding gas protection you have a brittle weak welds. Not to mention holes in your weld called porosity.

I cut the patch out with a cutting wheel. Some of the welds were actually pretty good, so I must have run out part way through the welding. I made a patch with a piece of paper and cut out a new patch out of 20 gauge steel. When I was getting the shielding gas at Chickasha Industrial I noticed they had a lot of steel in the shop area. Turns out they sell steel. So I picked up a few “cutoff” pieces for a good price.

The new patch with some help from a ingenious use of a 2×4 and a bottle jack fit nicely. I welded it in and it worked out pretty well. I struggled with one spot when the welding blew through a thin patch of original fender. With some creative welding I got the holes patched.

I still have to weld up the underside. Welding upside down is difficult. I’m going to have to figure out how to do that. Maybe watch some Youtube videos or something.

I will use the 16 gauge steel to reinforce the 20 gauge and weld in the seat belt mount. I don’t plan on having seat belts in the rear again but if I did, I’d need a place to mount them.

Thanks for reading and Happy Rovering.

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